Sorry for the delay in posting, but I was too beat after my pre-dawn stint to post.
Tim’s second stint was clean, as was that of Marcus, who went out after him. At the end of his second stint, the race was passed halfway, so Marcus brought the car behind the wall for scheduled mid-race maintenance. 25 minutes later, Sean reentered the track with fresh front brakes, bearings, and strut inserts. Some time during the night, one of the Dick Cepek lights quit working, but the other was working well enough that it wasn’t a problem. Yet.
Sean had another clean run, and after 70 minutes, he came in and I got back in the car. When I fired the car up after the fuel stop, the remaining Dick Cepek off-road spotlight failed, leaving me to run my whole 70 minutes with only the PIAA apex lights. I had another clean run, followed by still more poorly lit but clean sessions by Scott and Tim, who drove the car into the first light of day.
We had survived the night.
Marcus resumed the controls, and the Panhard rod broke yet again, sending the car behind the wall again for some therapy with the welder. After a short delay, we got going again, with Sean back in the car, starting the 4th rotation through the driver lineup. The standard 70 minute stint schedule was dropped at this point, as our position in the finishing order was unlikely to change, as there were 12-15 laps between the cars ahead of and behind us. The schedule was adjusted, to allow one more complete pass through the rotation, allowing Team Principal Marcus Miller to finish the race.
As Sean’s stint was drawing to a close, I was suited up ready to get in the car for my last session, I made my normal last chance bathroom break about 5 minutes before Sean’s scheduled pit window, only to return and find him on pit lane with what seemed to be another fuel pickup problem. It seems he hit pit road as soon as I left the pit box. Luckily Scott Miller was in the pit box, in his driving gear so all he had to do was pull on his helmet and hop in the car and go. I came back to the pit box as he was getting in the car. Sean reported that during his stint, the clutch had started slipping after 3rd to 4th gear shifts.
About 25 minutes into a scheduled 40 minute stint, Scott came back into the pits, saying “Something broke”. Ron quickly dumped in a can of fuel and Scott headed behind the wall, where after a brief investigation, it was found one of the bolts for the transmission crossmember had fallen out. A bolt was quickly removed from the Pro-7, and I hopped in to do my last stint. Scott reported the clutch was pretty much gone. My final stint consisted of nursing the car around in 4th gear the whole time, taking it as easy as possible, as the finish was in sight, under two hours away. The rear end had also developed a very unpleasant intermittent noise under braking. I managed to nurse the car around, where I handed it off to Tim for his final session. After he was strapped in and Ron dumped the last can of fuel into the car for the race, Tim turned on the fuel pump and ignition, hit the starter button, and nothing happened. No cause of the problem was immediately evident, the fuel pump was running, and the battery had voltage, so we push started the car on pit road, and Tim headed out on track.
Tim’s final stint was essentially the same as mine, but he did determine the grinding noise from the rear was probably coming from the LSD, as it only seemed to do it if you were trail braking. As long as you braked in a straight line, it was quiet. Tim left the car running for the final driver change, as Marcus got in the car for the final 20 minute limp to the checkered flag.
As the time ticked closer to zero, the crew nervously waited in the pits when Ron pointed out that every time Marcus drove by, the car was a little louder. An ugly exhaust leak had developed, and with about 10 minutes left in the race, the exhaust pipe broke in 2 pieces just behind the header, and the resonator and pipe were hanging under the car, nearly dragging on the track.
Marcus held out to take the checkered flag, finishing the longest closed course endurance race in the world. We finished 34th overall 15th in class, and completed 511 laps.
It was a blast.
Congratulations to the Lost 'N Spaced Racing Porsche 911, who took the overall win. I believe second place car was the SSF BMW M3, followed by the Car and Driver Subaru.
Marcus will have more later I am sure. I am going to bed.
Tom